1960 Crestliner: Phase 2

Last week we headed to Illinois four days earlier than the rest of the family to get the Crestliner running and comfortable for the 4th of July.

While we were gone I had a rebuilt outboard put onto the back of the boat. When the shop installed the outboard, they also replaced the rotten transom board for me.

When we started the project, we had an idea that we would pattern a new floor with painters plastic or butcher paper. This didn’t work too well. It was very difficult to keep the plastic tight on both sides on the curved edge. It was also impossible to reach both sides at once without being in the middle of them. We ended up doing side to side measurements every 6 inches to create a pattern.

Not perfect, but not bad

The subfloor of the boat had been filled with styrofoam, but throughout the decades, it had become water-logged, crumbly and moldy. When I looked up replacement options for closed cell foam, the slick mix and pour foam that would have perfectly formed to the subfloor troughs was far too pricey for this project. After googling several types of closed cell foam, we landed on pool noodles! $50 for enough to fill the whole thing.

We secured the floor over top by screwing it into the metal ribs.

The next step was the front seat. My father had a bench screwed down on all sides, but we wanted to make it open up to provide access to the storage we found underneath. This was obviously the original design since the hinges were actually welded in place.

We decided to cover the seat and the floor with a vinyl imitation teak decking. It’s soft on the feet, non-slip, pretty to look at, and it keeps you from getting splinters. After the flooring we took considerable time to install some swivel chairs. It was difficult because they bolted in both sides.

During the spring we made some cushions for the aft part of the boat using some closed cell foam and sunbrella leftover from our sailboat interior. Our next step was to make some bases for them. We chose to do a rectangular plywood base with 2x2s as joiners in the corners. After we had them all put together and painted, we traced them onto the floor where we wanted them. I then took them out of the boat and cleaned the plywood floor carefully before sticking down the vinyl decking. Then we bolted down the side seats and left the middle seat as a floater, which can be also be used as a step or a coffee table.

The last thing we needed was to get the lights running on the boat. That was fairly simple as the wiring isn’t very complex so we just ran all new. We ended up buying new stern and fore lights as well.

Our last obstacle was some safety concerns on the trailer. Our forward winch wasn’t working at all, so we got a replacement for it along with some new tires at the local farm store.

We did a quick test run in the yard, as well as some backing practice. The yoke of the trailer turned out to be a bit crooked, so pulling straight back involved a sort of S pattern wobble with the steering wheel to compensate.

Finally we got to take her down to the river! I can’t wait to take her out many more times in the future.

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Tips & Tricks for Installing a Lokar AOD Transmission TV Cable Kit

The 1967 Mercury Cougar project came with a 1980s Ford AOD transmission. This conversion is a nice upgrade over the original C4 if you plan to do much highway cruising.

OntheRoadAgain

However, the craftmanship of the original conversion left a bit to be desired. The person had used the factory AOD throttle valve (TV) cable, which didn’t really connect correctly to the carburetor. They had also fabricated a cable bracket and spring return that wasn’t holding up too well. I had noticed quite a bit of flex in it, and when I attempted to unbolt it from the intake manifold to investigate, it disintegrated.

TVCableBracketDisaster

The Lokar TV cable kit for AOD conversions came recommended from several different car magazines and forums online, so I decided to give it a shot. I won’t go into detailed instructions for the installation because there are a couple great videos about that already.

However, I will mention a few problems I encountered during the install and my solutions.

The first thing I did was add a Geometry Corrector to the Holley carburetor. While some people said they connected the Lokar cable directly to the carb with no issues, this piece creates an even pull from idle to WOT.

SonnaxGeometryCorrector

Then I tackled the transmission end of the cable. The shift lever went on with no problem, but the cable bracket was a trick. The Lokar kit comes with a longer bolt to replace the original pan bolt. It goes up through the pan and has a nut that goes on the back of it to support the tension.

LokarTVbracket01

On my car there was not enough space between the hole and the wall of the transmission to get the nut threaded onto the end of the bolt. If I had been doing this project with the transmission on a bench, I might have been able to hammer in the housing a little or bend the lip down a little to create enough clearance, but neither of those things were going to happen in the car. Instead I grabbed the dremel and shaved down the back edge of the nut.

ModifiedNut

With the flat side against the transmission case, I was just able to get it to thread. That stupid nut was the hardest part of the project.

Once I had the transmission end put together, I tackled the spring return bracket on the carburetor.

LokarReturnSpringBracket

The Lokar bracket that comes with the kit is really engineered for a throttle cable, so I had to adjust the bracket all the way in towards the carburetor, and it still barely has clearance for the throttle rod. However, the rod has full travel and the bracket isn’t causing any binding, so although I’d like a little more space, it seems ok. In the photo above you can see the Lokar adjuster tool that comes with the kit on the cable between the snap connector and the stop adjuster.

Strange fact, the allen wrench sent in the Lokar cable kit did not actually fit the set screw in the stop adjuster. I had to dig one out of my toolbox. Not sure how Lokar let that issue sneak past QA. Not a big deal, but then again, it’s not much of a confidence builder either.

Once the cable and all the brackets were installed, I screwed the pressure gauge into the TV test port on the passenger side of transmission and started the car up to set the TV cable tension.

With the car in neutral and absolutely no pressure on the cable, I was still getting 40 psi on the gauge. After several google searches and various tests, I finally pressed my finger against the shift lever and found it moved just the slightest bit. The gauge instantly dropped to 0. I let my finger off, and the lever slowly moved back out a few millimeters and the pressure came back up to 30 psi.

I have no idea why the lever wants to move by itself. This was not really discussed anywhere in any of the instructions. However, on some forums people had claimed that the Lokar cable spring wasn’t heavy enough to return their transmission to neutral while others defended it as being great. It definitely wasn’t strong enough for my transmission. I fabricated a little bracket and hung another return spring on the system, and suddenly, all my pressure readings were exactly where they were supposed to be.

LokarTVbracket02

I used vice grips to hold tension on the cable and tighten the set screw with the Lokar spacer in place to 35 psi.

PressureCheck

Then as soon as I pulled the spacer, the cable would snap back and the pressure would drop to 0 psi.

As soon as I removed the pressure gauge I took it for a test drive, and the shifts were much smoother and not as late as before.

One step closer to being on the road.

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